Yetti Posted September 23, 2017 Report Posted September 23, 2017 http://abc7.com/plane-crash-lands-on-glendale-street;-2-onboard-unharmed/2445414/ Quote
Jerry 5TJ Posted September 23, 2017 Report Posted September 23, 2017 Looks like it was N34BE a 1966 M20E. Quote
milotron Posted September 23, 2017 Report Posted September 23, 2017 Glad everyone is okay, but that must be a rare twin engine M20E... We were flying into Burbank, lost power to one of the engines for some reason, iain 2 1 1 Quote
bradp Posted September 23, 2017 Report Posted September 23, 2017 Looks like @chrixxer posted yesterday before this incident. Check in when you can. Thanks. Quote
neilpilot Posted September 23, 2017 Report Posted September 23, 2017 Glad everyone made it down with very minor injuries. Sold by Jerry Pressley earlier this year. Wonder if it will go back east for another rebuild? Quote
ragedracer1977 Posted September 23, 2017 Report Posted September 23, 2017 Sounds like everyone is OK. Made a couple calls to see if I could find out if he's OK. Waiting to hear back 1 Quote
Hank Posted September 23, 2017 Report Posted September 23, 2017 Well done, chrixxer! You passed an extreme test, the rest of college will pale in comparison. Please let us know what happened once the cause is determined. And take your brother on another flight to help him realize emotionally that it won't kill him. Quote
Jim Peace Posted September 23, 2017 Report Posted September 23, 2017 Awesome job....calm, cool and collected. I can only hope I would be half as good if that time ever came....... Did you fly it all the way through the crash like Bob Hoover suggested many times.................. Just yesterday in a hangar in Van Nuys my friends were giving me crap because I do not fly my C at night......... Quote
ragedracer1977 Posted September 23, 2017 Report Posted September 23, 2017 Got back word, he's in good shape 3 Quote
sleepingsquirrel Posted September 23, 2017 Report Posted September 23, 2017 Just how many engines did this Mooney have? Quote
peevee Posted September 23, 2017 Report Posted September 23, 2017 48 minutes ago, ragedracer1977 said: Got back word, he's in good shape Good to hear. Job well done. Quote
Yetti Posted September 23, 2017 Author Report Posted September 23, 2017 1 hour ago, sleepingsquirrel said: Just how many engines did this Mooney have? sounds like he needed n+1 3 Quote
MIm20c Posted September 23, 2017 Report Posted September 23, 2017 Not an ideal landing location...he did a good job! I’m curious what failed but glad he had his new radio in place for the emergency call. 1 Quote
steingar Posted September 23, 2017 Report Posted September 23, 2017 Damn, I can't imagine trying to put it down in a place like Burbank. Well done Chrixxer. And the Mooney roll cage saves another two. I'll take it over a parachute any day! 1 Quote
MIm20c Posted September 23, 2017 Report Posted September 23, 2017 1 minute ago, bluehighwayflyer said: At night over Burbank I would take the chute every time, personally. But agreed. Very well handled. I agree but in this situation I wonder if by the time he realized he had a serious problem if he would be too low. Quote
Ned Gravel Posted September 23, 2017 Report Posted September 23, 2017 Voice recording indicates he was at 1700' and still five miles out. That is at least three and one half miles too far to make it to Burbank airport (based on what my E model can do with a windmilling prop). Good work in a bad situation. Quote
AlexLev Posted September 23, 2017 Report Posted September 23, 2017 Job well done. Impressive. Glad he is ok. Quote
Bartman Posted September 23, 2017 Report Posted September 23, 2017 I only hope that I would be half as calm as he sounded. Bent metal, no injuries. Can't ask for better from the pilot under the worst imaginable circumstances Quote
Bob_Belville Posted September 24, 2017 Report Posted September 24, 2017 Great outcome and he sounded like a real pilot when the chips were down. I sure hope he didn't run out of 100LL. My first Mooney was on final to KAVL when my partner experienced fuel exhaustion engine failure too low to make the runway. Interstate 26 was no doubt easier to land on safely than a Burbank city street. Quote
MIm20c Posted September 24, 2017 Report Posted September 24, 2017 2 hours ago, Bob_Belville said: Great outcome and he sounded like a real pilot when the chips were down. I sure hope he didn't run out of 100LL. My first Mooney was on final to KAVL when my partner experienced fuel exhaustion engine failure too low to make the runway. Interstate 26 was no doubt easier to land on safely than a Burbank city street. I have a feeling he was renting the plane out. They talk about two college age people in the plane and I got the feeling that chrixxer was a little older. Glad nobody on the ground was hurt and the pilot did a great job putting it down. Quote
ragedracer1977 Posted September 24, 2017 Report Posted September 24, 2017 1 hour ago, MIm20c said: I have a feeling he was renting the plane out. They talk about two college age people in the plane and I got the feeling that chrixxer was a little older. Glad nobody on the ground was hurt and the pilot did a great job putting it down. No, it was him. He'll chime in here if he wants to, I imagine he's dealing with other stuff right now. Quote
MIm20c Posted September 24, 2017 Report Posted September 24, 2017 2 minutes ago, ragedracer1977 said: No, it was him. He'll chime in here if he wants to, I imagine he's dealing with other stuff right now. Roger that, I’m glad he’s ok! I’m sure he doesn’t have time to waste online right now. Quote
chrixxer Posted September 24, 2017 Report Posted September 24, 2017 (edited) I was the pilot. My passenger was a 2016 graduate of the same university/fraternity. If I’d had a chute I would have pulled it (we were ~1800’ AGL descending into KBUR when we lost the engine). My primary concern was my passenger and those on the ground. I looked for the darkest side street I could find (10pm in Glendale on a Friday night, the major roads were clogged with traffic). I just flew her until I couldn’t. In maneuvering to avoid an apartment building I (think I) stall/spinned her into a tree. That Mooney fuselage protected us very well. She wasn’t perfect, but she was solid. I’ve had her 4 months and flown her 65 hours (she was down for ~10 weeks getting avionics work done, which I knew when I bought her would be required), everything from pattern practice at Chino to 12K IFR trips to Utah and Arizona. Two A&Ps have worked on her. I’ll advise when I know more about what happened last night. All I do know is, as far as I know I kept in control of the plane as much as possible, and whatever skill I have as a pilot was heavily augmented by luck (no damage to property on the ground, no injuries). Now I’m sore, stiff, exhausted, and bowing out for at least a little while. I do believe I’ll have another Mooney someday though. Edited September 28, 2017 by chrixxer 18 9 Quote
Guest Posted September 24, 2017 Report Posted September 24, 2017 4 hours ago, chrixxer said: I was the pilot. My passenger was a 2016 graduate of the same university/fraternity. If I’d had a chute I would have pulled it (we were ~1800’ AGL descending into KBUR when we lost the engine). My primary concern was my passenger and those on the ground. I looked for the darkest side street I could find (10pm in Glendale on a Friday night, the major roads were clogged with traffic). I just flew her until I couldn’t. In maneuvering to avoid an apartment building I stall/spinned her into a tree. That Mooney fuselage protected us very well. She wasn’t perfect, but she was solid. I’ve had her 4 months and flown her 65 hours (she was down for ~10 weeks getting avionics work done, which I knew when I bought her would be required), everything from pattern practice at Chino to 12K IFR trips to Utah and Arizona. Two A&Ps have worked on her. I’ll advise when I know more about what happened last night. All I do know is, as far as I know I kept in control of the plane as much as possible, and whatever skill I have as a pilot was heavily augmented by luck (no damage to property on the ground, no injuries). Now I’m sore, stiff, exhausted, and bowing out for at least a little while. I do believe I’ll have another Mooney someday though. I'm glad you're alive to tell the tale. Engine out at night over a city, You did a fantastic job! Clarence Quote
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