So far , Pulled the interior , inspected the cage , sprayed the cage with corrosion-x , pulled the foil off of the splice plates , splice plates are clean , reinstalled interior ,removed sound insulation as it was pushing out the interior panels, repaired short in instrument breaker , Replaced KMA24 with KMA 28 , Replaced Apollo 618 and antenna , with Apollo GX55 and antenna , Replaced all the cowl fasteners with new , Disassembled mag , cleaned and adjusted points , set E-gap , cleaned and gapped plugs , Changed oil and filter and added Camguard (a case was in the plane ) , Replaced gear biscuits with 5 year old biscuits , Replaced exhaust tail pipe , Replaced glare shield with used one , Lubed the hell out of everything , Replaced ADF antenna , Reconstructed logs completely back to 2009 , Got airworthiness cert replaced , Ordered 3 new goodyear tires , Removed jugs for O/haul , Inspected cam lobes , performed SB208 , Annualed prop , replaced avionics lenses , scrubbed the living hell out of the plane , Cleaned K&N filter , replaced turn coordinator with used unit , rebuilt all 4 fuel caps , swung gear , Getting there slowly.......