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Everything posted by MooneyMark
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It was a comfy 22 degrees, in the sun at the beach it felt like summer!
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Just a short video to capture the vibe of a weekend to Texel (Island in The Netherlands).
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Recommendations on oil consumption next steps
MooneyMark replied to vance.k's topic in Modern Mooney Discussion
Folowing with interest, what does one do if you have your engine IRAN’ned? Send it over to the ayatollah? -
You can drop me a mail on mark.perlot AT icloud.com and I'm happy to send you my details.
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Not sure if you havent's contacted me already, I had contact with a someone from Switzerland earlier. I am willing to consider selling my 252, it's listed here: M20K 252
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Training has been slow the past six weeks, I did some practice runs to EHGG but this weekend I’ll be back at the flightschool. My dad passed away exactly one week ago, we operated the Mooney together and maintenance was completed just in time to do a very emotiononal farewel pass at his funeralservice. We both loved flying and we loved flying the Mooney together. He followed progress on maintenance right up to his passing and was thrilled to hear they finaly found a ‘smoking gun’ and the cause for the misterious oil consumption. I was in tears because at that time my dad was in the ICU fighting for his life and the doctors were still trying to figure out what was killing him. I said ‘dad, they fixed the Mooney, they will fix you too.’ Regretfully it wasn’t meant to be, he would have loved to take her up once more.
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This is the little spring we found in the oilfilter. I suspect this debris could also be to blame for the failure of the automatic wastegate, it is a hydraulicaly operated system.
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The e-mail my mechanic sent to Mooney and all other parties involved sorting my engine out. Maybe it can be of use for anyone else, so just putting it out there. Mind you, they checked the cilinders for oilleakage with an endoscope and had no reason to suspect the valvestem seals. ”Hi Guys, For a number of years we've been trying to solve the mystery of the oil coming from the exhaust tailpipe of a Mooney M20K with a TSIO360MB engine. (factory new 1989, 1168 TT, no major repairs been done to it apart from 1 cylinder change 2 years ago) Every time the aircraft was started up or flown the RH nose landing gear door and belly where wet of oil coming out of the tailpipe. At some point the turbocharger was changed. There was always about a cup of oil standing in the turbine housing. This didn't cure the problem. The one way valves in the oil system to/from the turbo where cleaned several times and eventually changed for new ones..... unfortunately no joy. We've checked the scavenge pump but it seemed OK. At some point the the starter clutch was broken and the complete housing was changed including the scavenge pump. We hoped that this would fix it..... No.... During a 100 hrs inspection some metal spring particles where found in the oil filter. Small bits like a lipseal spring. This gave me the idea to have a look at the intake valve guide seals since they have this kind of spring installed on the seals. I removed the valve springs and found 5 out of 6 seals being damaged. On 3 of them the springs where completely gone and on 2 others the seal was partially broken but the spring still in place. The only good seal was installed on a cylinder which I changed about 2 years ago. I guess that the one on the old cylinder was damaged too. I changed all 6 valve guide seals. Ran the engine and no more oil from the exhaust tail pipe. The aircraft has made several flights/starts since and so far good news. I thought this can be helpful to share. Greetings, Martijn”
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Magneto failure at 9000ft
MooneyMark replied to wings_level's topic in Vintage Mooneys (pre-J models)
Welcome WL, I'm not much help for you, had one mag failure but found out during run-up. I hope it all works out for you! For the other posters: how come the EGT goes up with one faulty mag? I'd imagine less mixture being burnt and thus a lower EGT...? -
Thanks again for you input, the wastegate moves freely and without any problems. It has been overhauled along with the controller by Main Turbo, the controller was sent back even, and replaced with another item. Great service from Main Turbo! My mechanic wil be on the telephone with Gary (Main) today, I hope he can shed some light on the matter. I've been doing some of my IR training now on a C172 now and that just isn't 'it'.
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Can't say that I did. I did a trial run yesterday and now the wastegate remained open, so I had to reject the take-off. I was suspecting that may be with a colder engine/engine-oil I might get the same results as I did Saturday (36" take-off and then a reduction to 25/26" WOT), but the wastegate remains open all the time now.
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Unfortunately I’m in need of your ideas again. My 1987 M20K 252 with just over 1000 hours total time is grounded for over five weeks now. It had some work done on the turbo due to the oil leaking from the exhaust. Nothing was replaced overhauled or repaired, save a few clamps. She flew fine for a few hours but she sits in the warm hangar of the maintenanceshop again. Take-off with full power and 36” MAP but just in to the climb the MAP drops to about 26” at WOT. What has been done? The turbo has been looked at and checked out okay, the output of the engine is okay, but the waste gate doesn’t seem to close. The controller and wastegate were shipped to Main Turbo for evaluation, the controller was out of spec and overhauled, the wastegate itself checked out okay but was overhauled anyway. Back on the engine, after some adjustments it seems to check out, but after a testflight yesterday we seem to be back at square one. I get full power at take-off but it drops off after rotation. Up in the air I tried different powersettings but did nog get more than 26”. That wastegate is not closing. I guess heat could have something to do with it? I tried another take-off after landing but had to reject it. I’ve read up on the subject with some of the great articles from Mike Busch (who doesn’t respond to e-mail BTW), six weeks ago I didn’t know what a controller was... do you guys have any thoughts?
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What Mechanical Faliures have you experienced in Mooney?
MooneyMark replied to 201er's topic in General Mooney Talk
In the air: autopilot u/s, transponder mode S became mode A only, more landinglights then I can count. On the ground: dead battery, magnetos dying, voltage regulator dead, oil squirting out from exhaust, starter dead/taking the (very expensive) starter housing along, cracked intake manifold pipe, fuel gauges dead and just recently discovered a groundwire with melted insulation running past the (leaking...) fuellevel sender unit while installing a fire extinguisher(!). That last one was nice, with the O2 plumbing running along the same route. Oh yes, a wastegate controller failure reducing my M20K to a normally aspirated model just after take-off... -
It appears to help to let the engine idle at around 1.400 revs a little while before shut-down. The last starts I had a clean gear door, but I'm not counting my chickens yet. Now waiting for the days to lengthen a little bit more so I can pick up my IR training again!
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I have the Clarity Aloft for two years now and am very happy with them. It's easy with sunglasses and oxygen and far more comfy! The bluetooth module I don't actualy use, only when flying as a passenger to listen to music or make a call. During flying it's only a distraction. I bought a set for my dad too and he wishes he had them sooner.
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After landing I let the engine idle for a few minutes to let the turbo cool, the mech suggested, since the turbo and ancillaries appear to check out fine, to let the engine run at 1400/1500 rpm for 30 secs before idle cut off. This allows for the scavenge pump to do its work better. Any thoughts?
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Just had call from the mechanic, the scavenge pump is good, as a matter of fact it is part (apparently...) of the starter assembly that was changed out for a new one early this year. The checkvalves are only two years old and have been tested. I'll have a chat later about the return hose, thanks! I was thinking if the scavenge pump is good, then maybe it gets too much oil for the pump too handle. Although the capacity of the scavenge pump should be 140% of the volume of oil being delivered. Can the flow of oil in to the turbo be regulated? It should be 3 qrts in and 4 qrts out,