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65C_flier

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Everything posted by 65C_flier

  1. Problem is fixed. It was either the fuel selector or the gascolator. On close inspection there was some slight blue fuel staining on the top of the gascolator bowl (shaw aero 1540-3), so a new o-ring kit was installed. The top of the fuel selector shaft looked pretty worn, but we ended up reinstalling for a ground run after the gascolator o-rings were installed and fuel pressure was good. Next flight, climbed to 8000ft and left the mixture rich. We saw about a 2 needle-width drop (to ~20 PSI), but assumed that was ok given the excessively rich mixture. Performed fine throughout the rest of the flight including go arounds. Noticed a few drops of fuel coming from the sniffle valve drain line (sump breather line) after the flight which I had never noticed before, but I assume that is unrelated and not a problem (normal fuel injector draining?)
  2. Thanks Skip. I had similar thoughts about the boost pump being downstream of the suspected leak so it shouldn't help, but the tempest video linked a few times in this post seems to indicate the additional pressure might blow enough through to effectively get the engine pump going (at 11min 35sec). That might also explain why it works for a bit after RPM reduction, but creeps back in. I agree there is still a good chance it is the engine driven pump, i just want to eliminate any easier options first.
  3. Hi all, I am having a fuel pressure issue with my 78J (IO-360A3B6D) that sounds similar to some of the issues discussed in this thread. I am hoping somebody might have experienced the same symptoms as me and be able to offer some advice before we go pulling too much apart. About 10 flights after my last annual I noticed that my fuel pressure on the ship's gauge during cruise climb with boost pump off was lower than its usual 25PSI (middle-of-the-green). It progressively got worse over the next few flights to the point where it dropped below the green (14 PSI) which really got my attention. Switching the electric boost pump on put the pressure back to around 23PSI. In cruise with boost pump off and leaned, the engine pump held around 23PSI. After some troubleshooting on the ground it was much worse than I thought. I took a video (that I cant figure out how to upload). At full power run-up the fuel pressure drops from 23PSI to about 6PSI and the RPM drops about 100RPM (from 2650 to 2550). Fuel pressure then oscillates between 6-10PSI as the RPM oscillates between 2550-2650 every 5-6 seconds. The boost pump puts the pressure back to 23PSI and stable RPM 2650. I had a look through my JPI data and I can clearly see the exact flight where this started. The graph below is an example from one of the later flights. The fuel flow starts to oscillate every 5-6 sec as soon as the boost pump is switched off. The EGTs follow. FF stabilizes for a few minutes when I reduce RPM for cruise climb, but then it returns. RPM is stable and I don't recall noticing the fuel px gauge oscillating at all during flight, but it is clear from the data that something is very wrong. The engine driven pump was overhauled a few years ago and there is no sign of fuel or oil from the drain line. No fuel stains around the servo or anywhere else. No loose fitting that we could find. My assumption is that air is being sucked in through a gascolator o-rings (which were replaced last annual) or the fuel tank selector. Interested in any advice before we go and pull those apart. I am also worried that the old Airight fuel selector (610289-007) will be difficult to repair or impossible to replace.
  4. Might have to give this a try. I've got 2 x 430Ws and the #2 unit has a "LOSS OF SIGNAL" for 1-2 mins about every second flight during climb out. On some occasions I have pulled up the satellite page on both units and watched the #2 unit slowly get signal back for each satellite shown on #1. Very rarely happens more than once on any given flight. It hasn't bothered me too much as the #1 unit is solid and I don't keep the database updated on the #2 unit anyway, but it sounds consistent with a loose antenna connection so it is worth a look.
  5. You will at least feel the yellow range vibration if it is a 79J with a 2 blade McCauley. I realise that is okay for non-continous use, but I try to avoid the yellow range for as long as practicable (until final). I guess the point is, there is no perfect number that covers all the possible Mooney variations. Know the POH and determine what works best forn your config.
  6. When you get time, you could go out and do some stalls in all landing configs you might use (flap land, takeoff flap and no flap) to validate your POH stall numbers at a high and low weight. Make a chart for 1.3Vso and use that as threshold speed for your specific flap/weight. 100kts (not mph) base and 90 base should usually work. Use the POH procedures for cowl flaps initially until you get time to analyse your specific aircraft behaviour, then adjust from there as other have suggested (easier to monitor it with an engine analyser). Cowl flaps seem quite dependent on the specific aircraft (e.g. condition of your baffling) and obviously DA, climb speed, etc. Recently I have found my OilT and CHT creeping up above my preferred limits on hots days in cruise at 24 squared (or WOT if higher). I might need some new rubber on the baffles and re-rig the cowl flap closed position open a bit more. The engine analyser alert at 400F CHT occasionally reminds me I have forgotten to open the cowl flaps during practice missed approaches on hot days...
  7. +1. First flight after buying a 78J with Century III I thought the elec trim wasn't working until reading the Century Manual. After figuring out how to use it I decided it was too course and it annoyed me disconnecting the ROLL or HDG modes if I needed to trim. So now I just trim manually and leave the elec trim switch off. AP still works in all modes including ALT hold. Trim switch still disengages all AP modes.
  8. I'd generally be more worried about the liquid juice than the electronic juice and I'd rather get on the ground quicker, so I'd usually keep it up and rely on the manual extension if required. I try to do the manual extension myself every annual and have a generally look at the motor/clutch/spring to add a bit of extra confidence that it is going to work when I need it.
  9. Good discussion. I've had a similar problem 2.5hrs into a 5hr flight and decided to head back to the origin where my A&P lived. The most concerning thing for me was having my Aspen EFD1000 detect low voltage and swap to it's internal battery which rapidly depleted from 100% to shutdown in less than 30mins. Made me pretty thankful for the VFR day and standby vacuum powered AI. I hadn't thought of a panel plug to ship's antenna for my hnadheld. Might look onto that.
  10. I usually takeoff at MTOW (family and full fuel). Doesn't seem to be a problem, but I agree staying at MTOW for the full flight is a penalty, as is stress on the airframe landing at MTOW.
  11. Hi all, Has anyone thought much about converting a Mooney to an electric motor? Might be a few years (decades?) away, but it seems like it might be feasible eventually. Some rough math for a J (using metric, sorry but its easier). Interested in whether anyone has thought more about it. 200hp (presumably at the output shaft) = 150kw. Electric motors are around 3x more efficient, but we still need 150kW going to the prop, so a 150kW electric motor is required Weight available: remove IO-360 engine 300lb, 64Gal fuel 384lb = 684lb (310kg). Might scrape together another 10kg in fuel components. Assume 50kg for (a theoretical 90% efficient) 150kW output motor, assume new prop same weight as old prop, 20kg for battery controllers gives 250kg available for batteries Power required for takeoff & climb (5 mins at 100% and 10 mins at 75%) = 31.25 kWh motor output (34.7 kWh battery input for 90% efficient motor) Cruise at 60% power = 90 kWh per hour of cruise (100 kWh input) Current batteries are around 250 Wh/kg or 4kg per kWh. Battery weight required: takeoff/climb 139kg, cruise 400kg/hr. With 250kg to play with that only allows 15 min takeoff/climb and 17 mins cruise (no reserve). Not very useful. Even if you throw another 200kg of batteries on the back seat, you only get 47 min cruise (no reserve). If (when?) batteries improve to 500 Wh/kg, that gets us to 54min cruise (no reserve) or 1.9hr (no reserve) with an extra 200kg of batteries. So it would take more like 2500 Wh/kg to get something comparable to what we have currently got (5.3hrs with 45min reserve). Charging rates would also rule out 2 long hops in a day, so we are probably never going to get anything comparable to what we have currently go, but I wonder what people's threshold would be to make it feasible.
  12. Good info, thanks Clarence. . The rod end I am looking for appears welded. I think I'll keep looking around for a used one.
  13. Does anybody know if it is possible to replace the rod ends on the MLG links like it is on the NLG links? Ive got a rear link, PN 550009-000 with a shot rod end bearing (from a 78J but I think it is common on most of the pre-80s Mooneys). Not sure what the rod end PNs are as the Parts Catalog doesn't list them separately.
  14. Thanks for the observations. The dark marks on the brake line are just grease/oil and good point about the safety wire. That pic was prior to removal and it was fixed on reinstall.
  15. Thanks Clarence. Super helpful as always. We didn't tap it out this time, but we will next time it is inspected. @mike20papa not sure what you are seeing here? The fuel lines going into gascolator looked OK to us.
  16. I sure have, but I cant figure out how to change my name Still on the topic of the A-1540. Can anyone tell me where the second MS29513-031 (the big o-ring) goes? According to the parts catalogue it is "between gascolator end plug (btm) and gascsolator housing". Mine only has the lock-o-seal washer on the end cap and there doesn't appear to be anywhere for the -031 to go. I'm wondering if I am missing something off of the gascolator housing? My A&P doesn't think so and the gascolator doesn't have any leaks, but it seems pretty strange.
  17. Geez this forum is great. I noticed my rudder stop was bent during annual today and was worried it was something serious. I guess somebody just bent it to adjust the stop... hopefully nothing to worry about.
  18. Ah, nevermind I found the kit https://lasar.com/seal-kits/complete-seal-kit-drawing-for-gerdes-silver-a-1540-gascolator-gerdes-gascolator-seal-kit-complete
  19. Does anyone know if the Brown Aircraft gasket fits the top (big) o-ring on this gascolator (78J)? I think it is the Shaw-Aero Gerdes circled below. The o-ring appears to be 1/16" with OD 1-15/16" which looks different to the Lasar 940057-001.
  20. Is there is supposed to be a drain hole in the bottom of the air induction box as shown in the picture (78J, but I assume it would apply to most models)? I guess it makes sense to drain water if it got in there somehow, but I would have thought the engine would always be sucking a bit of unfiltered air through there. We plan to incorporate SI M20-93 to remove the ram air, but we can't seem to get a kit. Looks easy enough to make the kit. Does anyone happen to know the thickness of thr blanking plate? I'm guessing around 0.032". Thanks.
  21. My MLG front trunion press-in zerks pull out as well. Has anyone tried oversizing the "drive-in zerk" hole and tapping to a regular 1/4" screw in?
  22. Exactly. If your J is in that SN range the only way to see it is from the top, and even then it is tough. Try shining a light down from outside. This is the best pic I could get.
  23. Yep, my 78J had a 2N2016 on the instrument circuit (likely original) which failed so the lights stayed full on or full off. The radio circuit had a different part number transistor, but same case. I can't recall that part number on thr radio circuit, but it didn't look original and the heat sink tray had been modified to allow easier removal. 2N2016 is obsolete and we replaced it with a 2SC5200N as suggested on a page here somewhere. It was quite difficult to do due to the location of the transistors behind the CB panel. In hind sight I would just replace it with a maxdim PWM and led strip. We replaced the heat sink (riveted to the tray) as the old one had big mounting holes that aren't very compatible with the 2SC5200N mounting. We also replaced the mica washer. The pic below shows the tray with the new 2sc5200n before it was reinstalled. It works, but we haven't done a lot of night flying since, so I don't know if it is a forever solution. I think later Js collocated the transistors with the rotary switches which would be an easier job.
  24. Thanks @EricJ. Yeah they did used to work although the glareshield lights were pretty intermittent before they failed on. I'm definitely considering maxdim next annual
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