They didn’t say. Only anomaly…there was one mounting bolt that was inside the cowling. Surprised it stayed in the plane, appears that it worked its way out at some point and maybe a bump on landing or rough patch of the ramp caused it to drop out and cause some bowing in the turbo, even that seems implausible as the TIT at landing was 1100 and for the three minutes prior below 1300 during descent. We have reams of engine data and we run the turbo below 1650, generally around 1615, but again, I doubt we will ever know the “cause”. That bolt wasn’t there the week prior when it came out of annual though they did find the left (as you are looking at it) clamp loose, not the the one subject to the AD. Could have been a lot of vibration. Could have been a bearing failure that caused the shaft to shift causing contact with the side of the inlet causing a bend. Could have been space aliens.