Jump to content

Gubni

Supporter
  • Posts

    134
  • Joined

  • Last visited

  • Days Won

    1

Gubni last won the day on October 24 2022

Gubni had the most liked content!

About Gubni

  • Birthday 06/07/1975

Profile Information

  • Gender
    Male
  • Location
    Jonesborough TN
  • Interests
    4-wheeling, cruising, and flying
  • Reg #
    N261TA
  • Model
    M20k 261
  • Base
    KTRI

Recent Profile Visitors

The recent visitors block is disabled and is not being shown to other users.

Gubni's Achievements

Collaborator

Collaborator (7/14)

  • Very Popular Rare
  • One Year In
  • Dedicated
  • Reacting Well
  • First Post

Recent Badges

116

Reputation

  1. He quoted me an exact measurement. Maybe 59" that it should be and mine is 58". I didn't take notes on the numbers, but his concern that it's one inch too short.
  2. I'm starting to get excited. Only one problem is keeping it out of annual. The main gear when extended is not verticle. We are going to put it on jacks and investigate that. It locks in position and has new pucks. I'm guessing this will be obvious when we start investigating it. The other problem is a minor oil leak. I don't know if it leaks with the engine running, but when parked it leaks onto the tire. My AI said it's coming from the internal altornator or oil filter adapter. Anyone else fought this problem?
  3. We made more progress today with a ferry permit to fix a few more minor details.
  4. Hehe, I'm sure he will understand it.
  5. While I don't understand most of that, I have sent it to my A&P as an alternate if he doesn't get the original to work.
  6. I tried and he said he didn't get it.
  7. It has the original tach and the jpi digital neither one work. Both sensors were left on the motor when it was sent off to be rebuilt and neither came back. The JPI was easy to order the replacement but still didn't work. The original was with Bendix maga and I have Slick mags and I can't find a direct cross over replacement. I ordered a generic version and I'm waiting to see if it works. .It is based at KTRI, but Greeneville is close.
  8. I got a local A&P to put on the SCAT tubing and work on some of the details. He didn't like the condition of the airbox and said that had to be fixed first. We got that fixed last week. I am hopeful that he will start trying to fix the tachs next. Once I get them fixed I will try to get the AI to finish the annual.
  9. I just replaced the engine and mounts on my M20k. My A&P said my old mounts are still in good condition so I thought I'd see if anyone wanted them. I have no idea if they have any value to anyone, but if someone needs them I'd rather see that then for them to get trashed. This board has been invaluable to me so I want to give back. I will auction these off. The auction ends November 30th at midnight. The highest bidder will send a donation to Craig McGregor to help support this board. Bidding starts at $20.00 They are pliable to the touch with no signs of dry rot. They are Lord mounts and there is a number stamped on one that says 12-86 which may be the manufacturer date. This plane has about 1600 hours since then. I suspect they were installed in 1990 when the prior engine was installed. 3 are part J-9613-76 and 1 is part J-9613-75
  10. Thank you for thinking of me. I already got one. It was a little over $1300 from LASAR.
  11. I got one from LASAR for a very good price. Thanks for thinking of me.
  12. It has been over steered and big dent in one of the tubes.
  13. No, that's all he found.
  14. Grounded at the last moment. I had a pilot with Mooney experience come by to fly it and he noticed this.
  15. Got it running today.
×
×
  • Create New...

Important Information

We have placed cookies on your device to help make this website better. You can adjust your cookie settings, otherwise we'll assume you're okay to continue.