Subtitle: The overhaul from hell...
Just got my M20J back from overhaul. Mind you this was after two test flights. The first flight, oil leaking from governor, we pulled it and overhauled it. Put it back on, second test flight was leaking from gasket. Replaced that gasket, third time was the charm and no leaks and I brought the Mooney back home.
Next weekend, I flew it about 8 hours, to and from Omaha and Oklahoma - performed great with no issues on the flight. After landing, taxi back, and shutdown was uneventful.
Skip forward a week and I go fly again. Engine start, taxi, runup was uneventful. Mag check was good. On takeoff roll engine sounded weird and like it wasn't making full power. I look down and see ~2200-2300 RPM. I abort the takeoff. A Couple of more static runs and it seems to be governed just above 2000 RPM.
I pull the cowl, check the cable and it seems to be making it to the low RPM stop just fine. I was sure it was the governor since it was having issues.
I have the governor removed and sent to the place that did the overhaul. They said it bench tested good...
Has anyone seen anything like this before? Looks like I'm pulling the prop to send it to the shop to see if there's something wrong with the prop. It seems that with enough RPM there is something leaking into the prop hub to increase the oil pressure to increase the pitch on the blades.
Attached videos show the runup. When I took this video, it looks like #2 cylinder dropped off (not sure if that was due to over boosting it or something else) but fuel flow and manifold pressure all looked good. #2 seems to keep good ignition the rest of the runs. I didn't want to run it too much over square. I also haven't checked the accuracy of the tachometer but it seems to be sounding like the prop is digging in and causing rough running.