Jump to content

InJuRo

Basic Member
  • Posts

    25
  • Joined

  • Last visited

Everything posted by InJuRo

  1. No, not really. 1. Did not see/feel any damage during preflight 2. While approaching, I deployed them and also checked visually through the window. Left one fine, right one "up". 3. While taxiing after landing (lower speed) it was "all down" 4. Back in the hangar I realized with a "wiggle test", that the inner mount is loose 5. Took of the lower belly cover and the small cover on the side and three screws, holding the flap mount (triangle) Shape to the spar, seems to be "loose" while still the paint marking on the nut is correct 6. I cannot access the head of the screw, so I have no clue actually, how to "tighten" them. Managed to tighten one and now flap is "good" again (wiggle test on the ground), but of course they all need to be tightened. Best regards and sorry for being a little unclear. Hard to describe. Ingo
  2. During my last flight with my M20E I realized during the visual check that my right landing flap did not "lower". The left one was fully deployed the right one was in some kind of nearly "full up" position. After Landing, while taxiing off the runway the flap was fully deployed. - Just to mention, flightwise it was no issue. I thought about putting the flaps back up but then (due to ice in the runway) took what I could get and it flew really well even with the flaps deployed differently. So far, so "good". After landing I checked the right flap and it turned out, that the inner flap mount, the "triangle shaped" bracked below the "step area" of the wing, was "loose". It could be moved a few centimeters/inches and as a result, the flap, even when deployed had so much "play", that the pressure pushed it back to the "nearly full up" position. I took the lower belly cover off and the little cover on the rear right side which is installed under this flap mount bracket. It seems like the bracket is mounted with three screws which are marked with red paint. These screws could be turned. They were not "loose" in a way, that the nut was loose (color markings were still good) but the did not really tighten the construction. I wonder if it may be a result of really low temperatures, age and the fact that alloy and steel expand and compress different. I would not like to tighten the screws/nuts. The problem is, that I can only access one side (the side with the nut) but not the backside. Did anybody ever habe this problem? I managed to "tighten" one nut with a mixture of a clamp and a wrench. And now the flaps has no play anymore. So this seems to be the issue. But of course I want to tighten (or if necessary exchange) all screws properly. Does anybody have an idea how to reach the "backside" of these screws? It does not work through the "handhole" which is close to it. This one only goes not to the complete back of the wing. Thank you for your help and tips Ingo
  3. Is the engine off with the engine mounting frame or without? I have the Laser kit and it installs very close to the engine mount/frame. How close also may also depend on your oil cooler. If you have "welding spots", sticking out on the outer housing of the oil cooler, it gets even closer. If the housing of the oil cooler is flat, it is easier. I put some leather in between, to see if there is any contact during vibration. Installation takes "a motivated weekend". When the engine is installed, attaching the rear mounts of the baffles ist no joy. This may be much easier with the engine off. Nevertheless when the engine is off without the mount, be aware to retrim, when installing the engine. When you have the oil cooler installed, consider to close the gaps on the side with either e proper instant seal or bend yourself some aluminium which you mount in. The better airflow will drop oil temp by a few degrees. Otherwise with the relocation it felt like the oil gets a little bit hotter. Get a good and sharp drill to get rid of the rivets of the former oil cooler mounting frame at the front cowling. Ingo
  4. The Vent line goes to the belly of the front cowling and then ends "in the air", so that fuel simply "gets out". There is no connection to anything on the other side after it went through the firewall. Ingo
  5. Increase in this case means that the indicator moves "down" or "up". I am not totally familiar with the mechanical construction of the instrument but if it moves "down" when you put the switch on, really check if it is simply connected the wrong way around, meaning vent and pressure port were mistaken. I add some pics of my old instrument. I also did a short test and blew (with the mouth) some air in the vent port connection. Et voilà! This caused exactly what you indicated, the needle reversed (went to the left). So I guess there is a high chance that one of the connections is wrong. There are ports on the back of the instrument, which are labeled MAN (Manifold), FUEL (Fuel in) and VENT (Fuel Vent port). They may be misconnected there or at the connection which goes through the firewall and will normally be slightly on the right half of the firewall (sie top of arrow). Ingo
  6. Propably not without modification. The Shower of Sparks has an extra Pin on the Bendig switch which is activated either when you "push" before turning to starter or with some other models just when you turn the starter. The Shower of Spark connector is marked with "BO" (Booster Output). You can find it in the installation manual for the Bendix TCM Switch 10-357210-1. This is a nice manual to the ignition switch. http://www.aeroelectric.com/articles/Shower-of-Sparks/ShowerOfSparks.pdf You can find the different connection "modes" on page 11. So I guess you'd need a switch which can ground the shower of spark at a certain mode. In the installation manual of the Ignition Panel, the shower of spark system is not mentioned and it seems like there is also not connector for it. http://www.electroair.net/pdfs/EA13000IM.pdf Ingo
  7. Tomorrow my new seats will come. When they are back in, I want to do an oil change anyway and I will "taste" the oil The cowling is dessert dry inside. Oil filter was not oiled when the engine was changed. But we will see, when it was running. Thanks for all your help.
  8. If I remember correctly there are two fuel lines on the back of the instrument. One to the instrument and one "vent line" back through the firewall which should end somewhere on the belly in front of the gear. In case the inner membrane of the instrument brakes and the fuel "passes through" it is then cleared through the vent line. When the EMS was hooked up, did you you use the same fuel pressure port for both instruments?
  9. As it is not yet running (interior is redone) I can only send the pic of the air filter bracket so far. On the side view (left picture) you can see the "non-optimal" fit (was the same with two different cowlings). On the other picture (right one) you can see where the oil "runs" after shutdown (shiny spot left) which is the side of the filter facing the front gear. Will take some more pics as soon as practical. Ingo
  10. One more thing.... Does it change when you turn the electrical pump on?
  11. Did you change any other connections? Both instrument are connected through the firewall and with the older Mooneys the fuel pressure may be taken from the distribution spider on top of the cylinder. There the pressure at the spider distribution port is lower than at the fuel pressure port, so if connectors or tubing were changed, there may be a wring pressure for the instrument and it goes on "max"? I had this issue when I got an EDM. When you connected it to the former pressure line of the instrument, the reading was minimal as pressure was taken from the distribution spider. Do you have a EDM installed? Ingo
  12. @carusoam Thanks for the input. EDM-Data is all good (EDM 900). Mag-Tests are smooth. No white smoke, neither with start, nor at any other time. Turbo is dry like a dessert. It definitely comes "from the top", so from the Rajay Airbox. I like this challenge also (even as it tends to be a little bit annoying) @N201MKTurbo Santa Barbara sounds like a good option. Cold and Rainy here in Nuernberg, Germany. The air filter has the inner bracket with the filtering mesh and an outer "mount" which with the Challenger consist of a rubber seal and a flat metal frame which is screwed on the cowling with six screws. The production quality of this mount is moderate at least and the shape does not fit perfectly to the cowling. There is no risk of dirt or dust getting in as the inner filter bracket fits "tight" to the side of the cowl but the rubber seal does not prevent any oil from passing by. I will try to take a pice. Just may take about 1 1/2 weeks as I am getting the seats redone.
  13. My Mooney M20E actually has an Astronautics Pathfinder Autopilot but will go for a Garmin GFC500 soon. As I already have the side panel out, I want to route the wires to the servos already, so that they are prepared and I do not have to take it out another time then. Can anybody tell me where in the wing the aileron servo is installed? Will it be at the same place where actually the Astronautics Pathfinder Servo is placed? I found how the ones in the rear are installed so it is no issue to prepare these cables already. But I wonder about the place in the wing. And concerning the Canbus-Cable do you know if it was terminated in the wing, so the wing servo is the final one or wether it is common to route from the panel to the aileron servo and then continue to the servos in the rear? Ingo
  14. I think my connector of the ADF Antenne in my M20E looked like this. Do you have a fitting "hole" (which may have been covered) in the belly underneath? @N201MKTurbo was faster I guess Ingo
  15. I will check for the issue Jim described. But as is is the same filter as before, I can hardly imagine why it should drip now besides maybe that the temperatures due to the normalizer installation got higher and therefore the oil now partly drips. On the other side, I had taken the oil filter away and the oil was in the upper air chamber of the Rajay (directly oder the oil filter). As the oil may not "jump up", it has to come from the top. The engine has absolutely no "white smoke". It runs clean. Absolutely no oil on the belly and no oil at the tail pipe. So far I do not find any oil missing. The engine uses little oil. I found in the Bonanza-Forum that this seems to be common with some engine and may be gone over a while or maybe not. There are some who write that even after 600 hours, there is still some oil dripping and some that say after 20-30 hours it is gone. They explanation was that this is conservation oil. On the other side it was also written, that these may be leaking valve guide seals. But shouldn't there be white smoke then? I guess next is to take off the lower cowling and take a good look into the intake system. Ingo
  16. Thank you for this suggestion. I didn't have this kind of valve in mind. Will check for that.
  17. The Case My Mooney got a (pretty) new engine, IO360A1A with a normalizer which was overhauled about 42 hours ago. I love the engine. After 30 hours it was uninstalled from the former aircraft it was filled to the top of the crankcase with oil (about 14 qt) and then stored properly. It also has a normalizer. Between the disassembly and the new assembly in my mooney it was stored properly for about 16 months. I got it installed, added as surely and flew for about 12 hours now. The engine runs very well, besides it is a little bit rough at lower RPMs (magnetos and so on were checked). Temperatures are all in the green, EGT/CHT spread between the cylinders is minimal, power is good, it is obviously using no oil , there is no white smoke, no oil in the exhaust and no oil in the breather tube. The belly and everything under the aircraft stays clean. The Problem and the symptoms But there is one exception. After I shutdown, some oil drips from the air filter. I have the M20E, with the air filter in the middle of the cowling and actually there is a Challenger air filter installed. The amount dripping is approximately 15-20 drops. Visible but nothing serious. The dripping oil is (already) cold directly after shutdown. It looks "fresh" and has a nice golden appearance. The oil in the oil pan also looks fresh after the 10 hours (golden). So I think there is no blowby. The oil also does not smell "burned". The oil does not come from the normalizer, as intake and pressure side of the turbo are perfectly clean. So I am sure there turbo does not overflow in oil. Also all valves to the Rajoy are installed properly and the flow test of the scavenger pump is fine. After uninstalling the air filter I found out that it seems like the oil comes from the intake/fuel mixure as it seems to run through the pipe from the Rajay Airbox (behind the little flap) to the mixer. One factor which may be of interest is, that during take off, with oil about 120° Fahrenheit my oil pressure is really high (up tp 105 PSI) while with "hot oil" at around 180 - 190° Fahrenheit oil pressure is in the middle of the green. But looking in the Lycomin maintenance manual I cannot see any oil line which may be able to leak to the intake due to high pressure. What I checked and considered to far I checked what could be the cause: Worn/broken pistons rings: But power and pressure as well as temps are good on all cylinders. There is no blowby. Not burning oil. Belly of the plane is perfectly "dry" and no relevant oil (not linke my older engine which spit a lot on the belly). Worn or not proper sitting intake valve: But this would not explain, why it drops as the oil had to come from somewhere and in the cylinder there is normally no oil which could then be "pushed" in the intake I guess. Also there is no plug fouling or anything. Colors of spark plug is nicely "light brown" Turbo overflowing: Lines to and from the turbo are perfectly dry. I now checked the Lycoming manual and the pipes for the intake go directly through the oil pan. Nevertheless there is no "physical connection" and no "seal" and if there was a leak or sth (like a crack) I'd expect that oil is running pretty much all of the time or at least if it was temperarture related it had to "drain" during flight, either in the cylinder (being sucked there with the air) or significantly more in the intake system. I'd also expect that I have a significant oil loss then. Actually it was I guess about maybe half a qt in 10 hours what I lost while flying. I also wonder if it may be some kind of "rest" after the engine was drained in oil (14 qts) for storage. Then it should be gone after a while but I have no clew how long this would take. Does anybody know if 14qts is enough, so the cylinder was in oil totally and some oil could have left through the intake pipes and may now be dropper in the intake? A factor may also be the challenger air filter. Its side seal to the cowl is very poor and this is where the oil "drops" out. As the amount is little with a better seal and maybe with the "old air filter" it may not even be visible. But still I did not have it with my old engine (and the same air filter). The oil dripping also seems to be a little bit "gluey" so it has some kind of "glueing" consistency, a little bit like "camguard". And it is "cold", so even directly after engine shutdown when it slowly starts to "drop", it as no relevant temperature. The Quest I talked to different mechanics but so far did not get any satisfying answer besides wait and see. Does anybody have an idea what to check next and what may be the reason? Did anybody discover sth like this already? Or does the swarm intelligence of the forum finally agree, that it may just be a matter of time until it is all "drained" and little sums of oil make a big mess?
  18. I think so also. There was no contact to José before the order. I had contacted @Gagarin after the purchase hoping for some more information (e.g. if @Shaune ordered with him, as I was always told, that the order was placed but José could not yet deliver). Did not get a reply from José so far, but still I agree, that the guy who got my payment, ist responsible. Before ordering I did not have contact with José. I dealt with EMAPA and it should be admitted that firstly they only wanted to install the kit but finally (I think with some extra "handling" fee) we agreed, that the kit will be sent to Europe finally. But this was two years ago. I'd be interested to know, If the order was really forwarded to José and - what is not problem - we'd be still in "his" waiting cue due to his sickness. This was what I was hoping to get to know from @Gagarin. If the order was not placed with him yet, this would cause a serious concern. If the ordere was placed but @Gagarin could not yet finish the STC due to health issues, it would still not be nice but I'd be finde with this. Nevertheless, then it should somehow be clarified that in case @Gagarin was already payed by @Shaune in case the STC may never be finished, it is secured, that we get the payment back from whoever finally got which amount. All this is even stranger, as I was in San Marcos about three years ago, when we visited the Mooney-Factory in Kerrville and stayed in Austin an San Antonio. So for me this was more or less a reason to "trust". Been there, seen it, looked like a good general concept (EMAPA).
  19. I tried in december, but no reply either. Mailbox says, that it the mail was not even "read". Has somebody ordered sth recently with EMAPA? Website seems to be still online and I got the impression that it was partly renewed. But as there is no reply I wonder if maybe they are out of business?
  20. Sorry, to bring this topic back up. But again there is absolutely no reply so far, neither from Jose (contacted him by mail and by PN) nor from EMAPA / Blue Sky Aviation. Does anybody have some recent experience or contact with one of them? About two years ago, we had payed a little bit more then 8.000 $ so it is a real issue that there is absolutely no communication anymore. Now I got some Mail-Errors, when replying to some of the older mails ("Diagnostic-Code: smtp; 554 5.4.7 [internal] exceeded max time without delivery"). I am seriously thinking about legal consequences but also do not want to case an unnecessary mess. Thx in advance for any help with this issue. Ingo
  21. Thank you for your answers. It is the swivel joint of a M20E which ist used to connect Mixture and Power Lever to the fuel injection unit. Checkten the Lasar-Webpage but did not find that part. Will write to Dan and check the alternative. Ingo
  22. Does anybody know, where to get the castle nut for the swivel joint 660051-3 as shown on the picture? Searched the web for quite a while now and found some used swivel joints but actually I'd only need the nut as mine as some "lost teeth". Ingo
  23. Hi, does anybody have any actual experience with EMAPA / Blue Sky Aviation in San Marcos, TX? In Januar 2019 we purchased to Monroy Long Range Tanks for a M20E and a M20K. We payed a few thousand dollars. We were told that the owner of the STC was sick or had a stroke so there will be a delay. The delay now lasts for about 1 1/2 years. I called there multiple times but reached only the answering machine. The last mail contact was in January 2020. We offered to come over - thx to Covid 19 this is an issue actually as we are from Europe - but no replies. Does anybody have experience if they are still in business and if we need to expect to take legal issues to get our money bag? I'd gladly wait for the Monroy's if there is a delay due to health or other reasons but at least a regular status update would be appropriate due to the money that was already payed. Alternatively at least the money should be refunded. If anybody has some information he does not want to share in a public forum, I'd be happy to receive an pm. Thx
  24. If it will get back, I'd gladly buy it.
×
×
  • Create New...

Important Information

We have placed cookies on your device to help make this website better. You can adjust your cookie settings, otherwise we'll assume you're okay to continue.